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  Mustangsandmore Forum Archive
  '64 1/2 to '68 1/2 -- The Classic Mustang
  CARB! I don't know what I am doing. I blew it up.

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Author Topic:   CARB! I don't know what I am doing. I blew it up.
rmousir
Gearhead

Posts: 1124
From: Amelia, Ohio
Registered: May 2003

posted 05-27-2006 05:16 PM     Click Here to See the Profile for rmousir        Reply w/Quote
Ok. I know I am a rookie but I am really starting to think I have no idea what I am doing and I just blew up my carb to back up that thought. I bought the power valve as was earlier mentioned. Put it in. No problem. Put the carb back on the car. Bolted everything up. Got the car started. The rpms are high and then the car dies. I figure that this is due to the car not being warmed up. I do this a couple of times. turn the key by reaching in the car. The car starts. Then by using my thumb I give the car a little gas. I am not revving to high rpms. Then BANG! a very large bang. Scared the crap out of me.


Now the carb is broke.

What am I doing wrong? I took a perfectly good carb and blew it up.The dist is good. It is in the right tooth. It may be a little advanced or retard but I am not sure. No vacuum leaks. The adjustment screws are 1.5 turns out from closed. The idle screw is 1.5 turns. I have not touched anything else on the carb.

Now what should I do? I am very frustrated with this part of the project. I have come so far. To make matters worse I was really hoping to drive it this weekend. Now it will take me most of the summer before I can come up with the money to buy another carb. I do have a two barrel I can put on there. Maybe I will do that. Still I am very very disappointed with my actions. I am my biggest problem.

Any ideas are greatly appreciated. Just don't know what to do.

Thanks for listening to me ramble. The weekend is going to suck.

Richard.

------------------
rmousir
'66 Mustang Coupe
Ford Blue & white stripes
'95 302 auto
Mustang ~ 04-05

[This message has been edited by rmousir (edited 05-27-2006).]

johnmustang
Gearhead

Posts: 6748
From: British Columbia , Canada
Registered: Nov 2001

posted 05-27-2006 05:23 PM     Click Here to See the Profile for johnmustang        Reply w/Quote
I am by no means a pro or even close to it, but if the carb keeps popping and back firing and so on that would indicate at least to me (a huge amateur) that it is your ignition (dist, timing, coil and so on) system causing the problem.

I will wait along with you for the real mechanics to show up and teach both of us what is wrong.

------------------
JOHN
65 FASTBACK 2+2
87 TAURUS WAGON
03 F150 XLT SUPER CREW 4X4 SHORT BOX
Member: PACIFIC COAST MUSTANG ASSOCIATION
Member:Vancouver Island Mustang Association
M&M #1710
65 FASTBACK
2003 F150 XLT SUPER CREW 4X4

Aussie XAXB
Gearhead

Posts: 131
From: North Olmsted, Ohio
Registered: Jan 2006

posted 05-27-2006 06:08 PM     Click Here to See the Profile for Aussie XAXB        Reply w/Quote
What carb was it? The Holley 1850 has a reputation for back firing at low RPM when you rev it. There is a fix for that but I would let a pro do that for you.

A backfire can also be a mixture problem or a timing problem. Very few things that go wrong with an engine have only one thing that can cause it.

You may want to get a book and read up on carbs if you want to work on them. Magazines have some really good articles too.

Scott H
Gearhead

Posts: 1480
From: Chicago area
Registered: Mar 2005

posted 05-27-2006 07:14 PM     Click Here to See the Profile for Scott H        Reply w/Quote
quote:
Originally posted by Aussie XAXB:
What carb was it?

It WAS a 4100 with a fresh clean and rebuild.
I supplied it, and I've built dozens of them. Not saying it was perfect, but I really don't see what would have been wrong with it.
I would suspect the ignition spark occured while an intake valve was still open, allowing the flame to travel up thru the intake.


SteveLaRiviere
Administrator

Posts: 48752
From: Saco, Maine
Registered: May 99

posted 05-27-2006 07:15 PM     Click Here to See the Profile for SteveLaRiviere        Reply w/Quote
I think you guys are missing the obvious. Since the carb came off and the problem began when it went back on, that's probably where the problem is.

Most likely it's a vacuum leak, by the sounds of it a big one. Check the base gasket, perhaps it got ripped, or if you changed it, make sure it is completely sealing the base of the carb. Some manifolds have machined areas that don't leave much material left for sealing.

Check also for vacuum lines you left off, too.

Resist the urge to go 'adjusting' the carb or timing, that's the areas you can be sure the problem isn't, since you didn't make any changes to them before the problem started. Have patience and retrace your steps and you'll find the problem.

------------------
'70 Mustang Mach 1 - '70 Mustang Convertible - '72 Mustang Sprint - '94 F-150 XL

Fastymz
Moderator

Posts: 22791
From: Reno Nv M&M #1240
Registered: Apr 2001

posted 05-27-2006 07:19 PM     Click Here to See the Profile for Fastymz        Reply w/Quote
Steve, he had this problem before he worked on the carb.

http://www.mustangsandmore.com/ubb/Forum1/HTML/017024.html

------------------
oddly obsessed with big scoops on little Mustangs

HOOD HACKERS DELIGHT!
My Pics

Scott H
Gearhead

Posts: 1480
From: Chicago area
Registered: Mar 2005

posted 05-27-2006 07:33 PM     Click Here to See the Profile for Scott H        Reply w/Quote
quote:
Originally posted by rmousir:
.The dist is good. It is in the right tooth. It may be a little advanced or retard but I am not sure.

Richard,
Don't give up and don't be too disheartened. This is all part of the fun and challenge of working on an old car. You've conquered many other areas of the car and this is just another challenge to overcome.
You have mail.


SteveLaRiviere
Administrator

Posts: 48752
From: Saco, Maine
Registered: May 99

posted 05-27-2006 08:57 PM     Click Here to See the Profile for SteveLaRiviere        Reply w/Quote
quote:
Originally posted by Fastymz:
Steve, he had this problem before he worked on the carb.

http://www.mustangsandmore.com/ubb/Forum1/HTML/017024.html


Thanks Scoop, I didn't see that.

Wish I could be there to help you out.

The bang you describe above sounds like a lean backfire.

------------------
'70 Mustang Mach 1 - '70 Mustang Convertible - '72 Mustang Sprint - '94 F-150 XL

Scott H
Gearhead

Posts: 1480
From: Chicago area
Registered: Mar 2005

posted 05-27-2006 09:43 PM     Click Here to See the Profile for Scott H        Reply w/Quote
quote:
Originally posted by SteveLaRiviere:
Wish I could be there to help you out.

The bang you describe above sounds like a lean backfire.


I agree with both!

Scott H
Gearhead

Posts: 1480
From: Chicago area
Registered: Mar 2005

posted 05-27-2006 11:10 PM     Click Here to See the Profile for Scott H        Reply w/Quote
Richard,
Those numbers in the picture are the 7.5 power valve and the 49 jets in the front.

You will probably have to replace the power valve again after this blow-out. It looks like in the picture the carb body is okay, you might just need another top plate. Easy to change with a handful of screws and the air cleaner stud.

rmousir
Gearhead

Posts: 1124
From: Amelia, Ohio
Registered: May 2003

posted 05-28-2006 12:23 AM     Click Here to See the Profile for rmousir        Reply w/Quote
I have had the car running for such a short time. Now before the leak I have been able to drive it around the development. Although to do it I had to have the rpms up pretty high. It has not been driven since the. Total distance is maybe 3/4 a mile drive. Then I found the leak. So I fixed the leak.

When that was fixed I had it running again. Surging as it was before. Thinking it was the timing as many have pointed out I re-stabbed the dist by doing the thumb over the #1 plug hole. Then I also rechecked the wires to make sure they are correct. Then got the car running again.

The only real adjusting I have done is to the idle screw and the dist. Turning it to the left or right a small amount at a time to get the motor to smooth out when it was warm. I had all of the vacuum lines removed from my vacuum tree and had the tree plugged when I did this. When it was running and while I was thumbing the gas to keep it running I had wd-40 sprayed around the vacuum tree, the base of the intake, the base of the spacer, the base of the carb. Never heard or saw a difference of the way the car ran.

Then when the car was warm it back fired (1st time) up through the carb. Then, after I changed my pants, I went back to the task at hand. Just to get the carb to idle nicely. That never happened. A lot of run time (at least a hour or so) and then the back fire (2nd time).

I then changed my pants and decided to put it out on the forum here and see what was what. That is when the power valve came up. So I went out and got one. It was easy enough to swap out and I had no problems with it. Then today BANG!. This one was big and again, I changed my pants.

So I posted this thread and went out to eat and hang out with the family. I have just put on the old 2 barrel that I had on the old motor. I have a 2to4 adapter sitting here so I thought I would try it. Problem is I don't know if it will still work or not. I will start the car up tomorrow morning and see what happens. If it happens again I know that it is a timing issue or something other than the carb. If it does not happen and the motor runs fine I know it is the carb.

I feel much better after going out and walking away from the car. I am sorry if I sounded like a big baby when I posted this. I should have taken a break before posting. LOL.

I will let you know what happens tomorrow and go from there. Hopefully the 2 barrel carb will work and the motor will start and I will know which direction to go in.

Richard.

68mustang351w
Gearhead

Posts: 558
From: San Jose, Ca
Registered: Sep 2004

posted 05-28-2006 01:17 AM     Click Here to See the Profile for 68mustang351w        Reply w/Quote
quote:
Originally posted by rmousir:
I feel much better after going out and walking away from the car. I am sorry if I sounded like a big baby when I posted this. I should have taken a break before posting.


I think we've all been there, at least I know I have. Good luck, hopefully its something easy... David F.

DidgeyTrucker
Gearhead

Posts: 1813
From: Greenbrier, TN USA
Registered: Oct 99

posted 05-28-2006 04:34 PM     Click Here to See the Profile for DidgeyTrucker        Reply w/Quote
The idle speed is ALSO adjusted by the fast idle adjustment when the choke is closed. If this is out of adjustment it will prevent the normal idle speed adjustment screw from making any changes. I know tihs from experience.

If it backfires only when you open the throttle, check the accelerator pump. With the engine OFF, open the throttle and see if there are two streams of gas directed at the primaries.

Tracy

sigtauenus
Gearhead

Posts: 3969
From: Va Beach
Registered: Jun 2000

posted 05-28-2006 08:23 PM     Click Here to See the Profile for sigtauenus        Reply w/Quote
Just checking into this thread in the middle, but I would assume that Scott would have sent Richard the carb with the inital adjustments made and if it was a fresh rebuild there'd be no reason to suspect the power valve or an accelerator pump. I'm not pointing the finger at Scott, but going down the line of assuming that a freshly rebuilt carb by an old hand likely isn't the problem to begin with.

Every time I've had issues with backfiring its been timing related, not the carb. Sounds like there's been issues from the begining with getting this new engine going. I hate to suggest this as it means tearing her open again, but is there a chance that the cam gear/chain was installed one notch off.

For you experienced guys, how would you eliminate timnig error in the distributor from the cam/crank degreeing.

rmousir
Gearhead

Posts: 1124
From: Amelia, Ohio
Registered: May 2003

posted 05-28-2006 11:32 PM     Click Here to See the Profile for rmousir        Reply w/Quote
Originally posted by sigtauenus:
I hate to suggest this as it means tearing her open again, but is there a chance that the cam gear/chain was installed one notch off.

The cam gear chain was never removed. This is a motor from a wrecked '95 mustang gt. I never removed the timing chain and/or gears. I only added the eccentric. The motor was run tested before I bought it and I bought it from a reputable yard here in my local area.

I also agree on the part about the carb being top notch coming from Scott. I am sure that this is somthing on my part. Being new with lots to learn I am finding that I am the problem most of the time.


Originally posted by sigtauenus:
For you experienced guys, how would you eliminate timnig error in the distributor from the cam/crank degreeing.

I got the 2 barrel carb out. I will start the car up tomorrow and get it warm and see what happens. Will add a update tomorrow.

Richard.

rmousir
Gearhead

Posts: 1124
From: Amelia, Ohio
Registered: May 2003

posted 05-28-2006 11:35 PM     Click Here to See the Profile for rmousir        Reply w/Quote
quote:
Originally posted by SteveLaRiviere:
The bang you describe above sounds like a lean backfire.


What is a lean back fire?

Richard.

68mustang351w
Gearhead

Posts: 558
From: San Jose, Ca
Registered: Sep 2004

posted 05-29-2006 12:17 AM     Click Here to See the Profile for 68mustang351w        Reply w/Quote
quote:
Originally posted by rmousir:

What is a lean back fire?

Richard.



Not enough fuel in the mixture... David F.

Aussie XAXB
Gearhead

Posts: 131
From: North Olmsted, Ohio
Registered: Jan 2006

posted 05-29-2006 12:20 AM     Click Here to See the Profile for Aussie XAXB        Reply w/Quote
"The only real adjusting I have done is to the idle screw and the dist. Turning it to the left or right a small amount at a time to get the motor to smooth out when it was warm. "

Is this to say that the timing has never been set with a timing light, only by ear? Just looking to clarify that.

I would have to agree, sounds like Scott has built enough carbs to have a handle on what he is doing.

The timing chain could be off by one tooth because of "jumping", a phenomena that has been known to occur, usually really stumping the mechanic because it shouldn't occur. So even if the timing cover has never been removed the chain can still jump a tooth on it's own due to a misfire, backfire, or other event which will then cause a chronic performance condition.

bob6364
Gearhead

Posts: 447
From: griswold,ct usa MCA#59447
Registered: Dec 2004

posted 05-29-2006 12:21 AM     Click Here to See the Profile for bob6364        Reply w/Quote
are you using a timing light? or just going by what sounds good? Because you made a comment earlier that sounds like you just did a seat of the pants adjustment to the distributer.
I say use a timing light and then stick a vac gauge on the motor and adjust mix valves for highest vac. My 2 cents.

sigtauenus
Gearhead

Posts: 3969
From: Va Beach
Registered: Jun 2000

posted 05-29-2006 04:04 PM     Click Here to See the Profile for sigtauenus        Reply w/Quote
Yeah, the road I was going down initially was that timing chains get loose with age and that makes it almost impossible to set the timing without putting on a new chain, but then deleted that with the assumption that the 95 block had been rebuilt. I've not heard of late model engines having timing issues though.

SteveLaRiviere
Administrator

Posts: 48752
From: Saco, Maine
Registered: May 99

posted 05-29-2006 04:50 PM     Click Here to See the Profile for SteveLaRiviere        Reply w/Quote
My best guess from 2500 miles away and after reading your posts is that you have a massive vacuum leak at your intake manifold, the intake gaskets probably slipped down when you installed your new 4 bbl intake.

I bet you can't stall your engine by blocking the choke with your hand.

------------------
'70 Mustang Mach 1 - '70 Mustang Convertible - '72 Mustang Sprint - '94 F-150 XL

rmousir
Gearhead

Posts: 1124
From: Amelia, Ohio
Registered: May 2003

posted 05-30-2006 09:18 AM     Click Here to See the Profile for rmousir        Reply w/Quote
UPDATE!!

I got the car started with my 2 barrel carb.

NO SURGING at all!

Starts up just fine and is smooth but I can not get the car to run at idle with out stalling. I am starting to think more vacuum leak. Oh, also i got my nice new timing light. Bought a good one from Sears. Still, can't use it until the car idles right?

quote:
Originally posted by SteveLaRiviere:
I bet you can't stall your engine by blocking the choke with your hand.

Do you mean to cover the top of the carb with my hand to cut back the air? If so I will give that a try and see what happens. i will then follow up with everyone here. Should be tonight. Really want to get this fixed. I know I can do it.

Also wanted to say thanks to everyone who has been jumping in and helping me out. I really appreciate.

Richard.


------------------
rmousir
'66 Mustang Coupe
Ford Blue & white stripes
'95 302 auto
Mustang ~ 04-05

Blacksmith
Gearhead

Posts: 604
From: Front Royal, Va., USA
Registered: Feb 2006

posted 05-30-2006 09:54 AM     Click Here to See the Profile for Blacksmith        Reply w/Quote
quote:
Originally posted by Aussie XAXB:
The Holley 1850 has a reputation for back firing at low RPM when you rev it.

A backfire can also be a mixture problem.


Had the same problem with my old 600cfm Holley. It was running rich & backfired & bogged down when I stepped on it. I replaced the carb with a new one & that fixed it.
Haven't torn the old one apart yet to see what was causing it. Metering blocks maybe, or something internal???

"Turning it to the left or right a small amount at a time to get the motor to smooth out when it was warm."

Very true about the idle adjustment screw too. A little bit goes a long way.

[This message has been edited by Blacksmith (edited 05-30-2006).]

Scott H
Gearhead

Posts: 1480
From: Chicago area
Registered: Mar 2005

posted 05-30-2006 06:43 PM     Click Here to See the Profile for Scott H        Reply w/Quote
quote:
Originally posted by Blacksmith:
Had the same problem with my old 600cfm Holley. It was running rich & backfired & bogged down when I stepped on it. I replaced the carb with a new one & that fixed it.
Haven't torn the old one apart yet to see what was causing it. Metering blocks maybe, or something internal???

That may be true for a Holley, but this is an Autolite 4100 and they don't have metering blocks.

Richard -
First step is to get it running right with your old two-barrel on there. Fix the intake gasket leak if there is one, get your timing set at 10 degrees without the fast idle engaged and engine warmed up and vacuum advance disconnected and plugged.

THEN try swapping back the four barrel and maybe we can pinpoint what you need to do to the 4100 to smooth it out. Might be something as simple as a little bit of dirt got thru the filter (remember when you first tried to start it and the bowls flooded?).

Jake11
Gearhead

Posts: 246
From: Banning,Ca,USA
Registered: Oct 2005

posted 05-30-2006 08:44 PM     Click Here to See the Profile for Jake11        Reply w/Quote

Shure sounds like a vacumn leak. Could be
your intake gasket leaking underneath where
you won't be able to find the leak with
WD40. Do you have one of those propane torch
things for soldering? Propane works good for
finding vac. leaks, and it don't make a mess
like squirting WD40 all over. If you pull
the pcv valve out of the valve cover and
squirt some propane in the `hole, it might
show if you got a vac. leak. Good luck

KeithP

John Z
Gearhead

Posts: 506
From: Morgantown, WV
Registered: Jul 99

posted 05-30-2006 09:14 PM     Click Here to See the Profile for John Z        Reply w/Quote
quote:
Originally posted by rmousir:
Then when the car was warm it back fired (1st time) up through the carb. Then, after I changed my pants, I went back to the task at hand.
A lot of run time (at least a hour or so) and then the back fire (2nd time). I then changed my pants and decided to put it out on the forum here and see what was what.

Then today BANG!. This one was big and again, I changed my pants.

I feel much better after going out and walking away from the car. I am sorry if I sounded like a big baby when I posted this. I should have taken a break before posting. LOL.

Richard.


Sounds like your making progress, but this post made me think there may be a product that could help you spend more time in the garage
http://www.depend.com/

May be a good marketing concept.

68 Coop
Gearhead

Posts: 5847
From: Mesquite, NV. 89027
Registered: Oct 2004

posted 05-30-2006 10:13 PM     Click Here to See the Profile for 68 Coop        Reply w/Quote
quote:
Originally posted by Jake11:

Shure sounds like a vacumn leak. Could be
your intake gasket leaking underneath where
you won't be able to find the leak with
WD40. Do you have one of those propane torch
things for soldering? Propane works good for
finding vac. leaks, and it don't make a mess
like squirting WD40 all over. If you pull
the pcv valve out of the valve cover and
squirt some propane in the `hole, it might
show if you got a vac. leak. Good luck

KeithP

What do you look for, or will it die, surge... Sorry, I've never heard of this one before. I have a torch, and would like to see if I have any leakage anywhere. Thanks for any info on this.

------------------
William
The easiest way to find something lost, is to buy a replacement.

68 Coupe
289
C4
3:55's/Trac-Lok

rmousir
Gearhead

Posts: 1124
From: Amelia, Ohio
Registered: May 2003

posted 05-31-2006 08:29 AM     Click Here to See the Profile for rmousir        Reply w/Quote
Ok, Here is my plan.

Get the car running and put my hand over the butter fly and see if it stalls.

I should be able to close the butter fly and the car should stall right?

I will then check the intake seal again to see if I can find it. If not then pull the intake and super seal it.

Then put it back to gether and hopefully it will idle. Then set my timing at 10 btdc. If is smooths out with the 2barrel on then I will put the 4 barrel back on and see how it goes.

how does that sound?

I will have some time this weekend to go over it. If I have to pull the intake is there a sure way to seal it?

Richard.

68 Coop
Gearhead

Posts: 5847
From: Mesquite, NV. 89027
Registered: Oct 2004

posted 05-31-2006 09:48 AM     Click Here to See the Profile for 68 Coop        Reply w/Quote
Just make sure everything is very clean, let the silicon get tacky before you install the intake, and use it on the ends instead of the cork gasket pieces. I let mine sit for almost 2 days before I started it, just to be sure it had set up, but I don't know how long to wait in reality. Also Richard, when restabbing the distributor, make sure it drops in at the #1 spot on the cap, sometimes it can get off by a tooth and it will run like crap too. Luck

------------------
William
The easiest way to find something lost, is to buy a replacement.

68 Coupe
289
C4
3:55's/Trac-Lok

buening
Gearhead

Posts: 317
From: Decatur, IL
Registered: Mar 2005

posted 05-31-2006 11:24 AM     Click Here to See the Profile for buening        Reply w/Quote
Richard,
Maybe i can help a bit. First of all, what distributor are you running? Reason i am asking is because different distributors have different mechanical weights and just throwing out an initial timing number may work on some but not others. For instance, i have a duraspark dizzy with 10L weights, so i have 20° centrifugal timing. SBF motors like to run around 36° total timing, thus i have my initial set to 16°. One has to be careful, cause my first duraspark distributor had a huge weight, something like a 20L which is 40° timing and the car ran like crap. Anyhoo, just curious what distributor you have on there so we can get a good initial timing to set it at.

Also, you bought a vacuum gauge right? Hook that gauge up to the manifold vacuum tree and see what it is reading. This will let you know for sure if you have a leak. Sometimes the intake gaskets will leak from the inside of the motor, so the old carb cleaner trick won't work.

One final thought is the gas/filter. Do you have fresh gas in the tank and do you have a good filter after the pump? I had problems in the past with the cheap clear fuel filters that autozone sells. The filter is a plastic mesh and doesn't filter anything. I kept getting rust and gunk in my carb and it was blocking the passages in the carb, creating a lean condition and the car wouldn't idle under 1300rpms. Even though you put another carb on there, it could have gotten plugged up like the last one immediately.

One other thought, have you messed with the rockers or valvetrain at all? Just curious if the rockers were properly adjusted, as this can mess up the timing of the valvetrain causing backfires.

------------------
1970 Grabber Blue Mach 1 H-code
1970 Fastback
2003 Torch Red Mustang

68 Coop
Gearhead

Posts: 5847
From: Mesquite, NV. 89027
Registered: Oct 2004

posted 05-31-2006 11:33 AM     Click Here to See the Profile for 68 Coop        Reply w/Quote
quote:
Originally posted by buening:
do you have a good filter after the pump? I had problems in the past with the cheap clear fuel filters that autozone sells. The filter is a plastic mesh and doesn't filter anything.


Bastards, I paid almost 25 bucks for mine from there, if I remember correctly.

------------------
William
The easiest way to find something lost, is to buy a replacement.

68 Coupe
289
C4
3:55's/Trac-Lok

68mustang351w
Gearhead

Posts: 558
From: San Jose, Ca
Registered: Sep 2004

posted 05-31-2006 03:45 PM     Click Here to See the Profile for 68mustang351w        Reply w/Quote
quote:
Originally posted by rmousir:
I should be able to close the butter fly and the car should stall right?

Youre going to have to take the air cleaner off and put you hand over the top of the carb and block off as much air as possible. Simply closing the choke wont be enough... David F.

SteveLaRiviere
Administrator

Posts: 48752
From: Saco, Maine
Registered: May 99

posted 05-31-2006 08:27 PM     Click Here to See the Profile for SteveLaRiviere        Reply w/Quote
Yes, it should either stall or stumble like crazy. If it smoothens up, you've found a vacuum leak.

------------------
'70 Mustang Mach 1 - '70 Mustang Convertible - '72 Mustang Sprint - '94 F-150 XL

rmousir
Gearhead

Posts: 1124
From: Amelia, Ohio
Registered: May 2003

posted 06-01-2006 07:45 AM     Click Here to See the Profile for rmousir        Reply w/Quote
quote:
Originally posted by SteveLaRiviere:
Yes, it should either stall or stumble like crazy. If it smoothens up, you've found a vacuum leak.


I will run that test tonight. I will post my results back here tonight.

rmousir
Gearhead

Posts: 1124
From: Amelia, Ohio
Registered: May 2003

posted 06-02-2006 08:06 AM     Click Here to See the Profile for rmousir        Reply w/Quote
OK. Did not do the test last night. My little man (Cole-3 yr old) wanted to play hot wheels and he gets priority.

However I was reading my Tom Monroe book on the intake install to see if I missed anything. He mentions that I should have washers on the intake. I don't. I used the bolts from my '95 intake. If I do the test of putting my hand over the carb and if the car smooths out I have a vacuum leak. Would it be a good idea to put washers on the intake bolts?

I will be doing the test tonight for sure. Cole said he would help. What a nice kid. :-)

Richard.

68mustang351w
Gearhead

Posts: 558
From: San Jose, Ca
Registered: Sep 2004

posted 06-02-2006 04:06 PM     Click Here to See the Profile for 68mustang351w        Reply w/Quote
What kind of intake do you have ? If its cast iron dont worry too much about it but if it is aluminum it would be recommended... David F.

rmousir
Gearhead

Posts: 1124
From: Amelia, Ohio
Registered: May 2003

posted 06-02-2006 04:55 PM     Click Here to See the Profile for rmousir        Reply w/Quote
quote:
Originally posted by 68mustang351w:
What kind of intake do you have ? If its cast iron dont worry too much about it but if it is aluminum it would be recommended... David F.

Alum Offenhauser 360. I will put the washers on one at a time and see how she runs. Do you think it will make a big difference? How thick a washer should I go?

Richard.

68mustang351w
Gearhead

Posts: 558
From: San Jose, Ca
Registered: Sep 2004

posted 06-02-2006 05:43 PM     Click Here to See the Profile for 68mustang351w        Reply w/Quote
The only difference the washer is going to make is spread out the torque of bolt and since aluminum is softer than iron you should have those washers. Now that I think about it, grab youre torque wrench and check to see if any of the bolts on the intake are loose. Sometimes they loosen a bit after you first install them (because of heat cycling). If this did happen, it can create a vacuum leak. On my Edelbrock intake all the bolts are suppose to be torqued to 25lb-ft except for the 4 on the ends (2 front, 2 back). those only get about 15lbft, YMMV. Hope that leads us somewhere... David F.

rmousir
Gearhead

Posts: 1124
From: Amelia, Ohio
Registered: May 2003

posted 06-02-2006 10:28 PM     Click Here to See the Profile for rmousir        Reply w/Quote

Alright....

I got to do some testing on the car tonight. Here is what I have found. My intake was loose.... I tighten it up to about 30 pds according to my torque wrench. Then started the car and it made a difference. But it still ran really high on the rpms and then stalled. Started it again and then by thumbing the carb I took and closed the butter fly with my hand. WOW!

It changed the rpms a lot. I had to reduce the idle screw on the carb and the motor ran much better. If I let the butter fly open the rpms got really high and then the car stalled. Also with the butter fly close there was no surging. Remember that I have my 2 barrel on there now with a 2to4 spacer/adapter. I don't like it and I think it may be part of the vacuum leak.

So this means I have a vacuum leak right?

So what to do now?

I assume that I have to drain the coolant. remove the carb, spacer, pcv hose, the upper rad hose, etc, and pull the intake. Get a new set of seals and reinstall it after a good cleaning. Then put it all back on. Is there a fool proof way to do that seal so it does not leak? Again, I am assuming that the intake seal is the problem here. Special seal part number or something?

Then when I reinstall it should I torque it to the 30pds again? When I installed the intake I am almost sure I torque it really tight. I remember using my Tom Monroe book and I think it said somewhere around 80pds. Is that too tight? I am pretty sure that is what I did. How did it get so loose? Should I go tighter than the 30 pds? Also I did not put on the washers.

Then I will get the 4 barrel carb back on there and get new seals for it also.

Still need lots of help on this one, I really want to drive the car this summer.

Richard.

johnmustang
Gearhead

Posts: 6748
From: British Columbia , Canada
Registered: Nov 2001

posted 06-02-2006 10:53 PM     Click Here to See the Profile for johnmustang        Reply w/Quote
quote:
Originally posted by rmousir:

When I installed the intake I am almost sure I torque it really tight. I remember using my Tom Monroe book and I think it said somewhere around 80pds. Is that too tight?

Richard.


If you did 80pds I think that is way to tight and that is probably your problem. Here is a link that will help you.

http://dfwmotorsport.com/Fairlane/Manifolds.htm



------------------
JOHN
65 FASTBACK 2+2
87 TAURUS WAGON
03 F150 XLT SUPER CREW 4X4 SHORT BOX
Member: PACIFIC COAST MUSTANG ASSOCIATION
Member:Vancouver Island Mustang Association
M&M #1710
65 FASTBACK
2003 F150 XLT SUPER CREW 4X4

rmousir
Gearhead

Posts: 1124
From: Amelia, Ohio
Registered: May 2003

posted 06-02-2006 10:56 PM     Click Here to See the Profile for rmousir        Reply w/Quote
quote:
Originally posted by johnmustang:
If you did 80pds I think that is way to tight and that is probably your problem. Here is a link that will help you.

http://dfwmotorsport.com/Fairlane/Manifolds.htm


Thanks. It was loose when I got to it tonight. I dug through my book and I have a copy of that page in my book and now that I have seen it I think I may have done it that way. That would explain why the bolts were so loose. If it were 80 pds I don't think they would have gotten this losoe. It is about 30 pds now.



[This message has been edited by rmousir (edited 06-02-2006).]

johnmustang
Gearhead

Posts: 6748
From: British Columbia , Canada
Registered: Nov 2001

posted 06-02-2006 11:41 PM     Click Here to See the Profile for johnmustang        Reply w/Quote
quote:
Originally posted by rmousir:
Thanks. It was loose when I got to it tonight. I dug through my book and I have a copy of that page in my book and now that I have seen it I think I may have done it that way. That would explain why the bolts were so loose. If it were 80 pds I don't think they would have gotten this losoe. It is about 30 pds now.


You may have compressed the gasket, it could have slipped or you could also have a crack on the intake.

Are you having any overheating problems? After you have run the car for a little while, remove the rad cap (very carefully) and see if you can smell any exhaust fumes coming from the rad, if you can then you definitely have a problem with the intake.

------------------
JOHN
65 FASTBACK 2+2
87 TAURUS WAGON
03 F150 XLT SUPER CREW 4X4 SHORT BOX
Member: PACIFIC COAST MUSTANG ASSOCIATION
Member:Vancouver Island Mustang Association
M&M #1710
65 FASTBACK
2003 F150 XLT SUPER CREW 4X4

rmousir
Gearhead

Posts: 1124
From: Amelia, Ohio
Registered: May 2003

posted 06-02-2006 11:45 PM     Click Here to See the Profile for rmousir        Reply w/Quote
nope. no overheating at all. I will pull the intake tomorrow and start the process of redoing the intake. I have some tips on how to do it from ScottH.

I will do that and then post my results. Hopefully they are better.

Thanks.

Richard.

Jake11
Gearhead

Posts: 246
From: Banning,Ca,USA
Registered: Oct 2005

posted 06-03-2006 03:03 PM     Click Here to See the Profile for Jake11        Reply w/Quote

When you put it back on, tighten the bolts
a little at a time starting with the center
ones first and working out to the ends. That
way it won't distort the gaskets. 22lb's
is what it says in my Mitchell man. Those
bolts will break in half if torque them to
high. Good luck, KP

SteveLaRiviere
Administrator

Posts: 48752
From: Saco, Maine
Registered: May 99

posted 06-03-2006 06:13 PM     Click Here to See the Profile for SteveLaRiviere        Reply w/Quote
Sounds like you're getting it. Once you get that intake back on there right I think you'll feel like you have a new engine.

------------------
'70 Mustang Mach 1 - '70 Mustang Convertible - '72 Mustang Sprint - '94 F-150 XL

crawlerchris
Journeyman

Posts: 11
From: Space Coast , Florida
Registered: Jun 2006

posted 06-03-2006 07:52 PM     Click Here to See the Profile for crawlerchris        Reply w/Quote
Ive seen backfiring problems with craptastic running on a engine that had a missing pushrod before . It had bent the pushrod and fallen off the rocker arm joint so it was not opening the exhaust valve .

rmousir
Gearhead

Posts: 1124
From: Amelia, Ohio
Registered: May 2003

posted 06-04-2006 08:46 PM     Click Here to See the Profile for rmousir        Reply w/Quote
So this is what I found. When I took off the intake I totally remembered what I did. I used the silicon on the water passages and not on the fuel passages. So that was my mistake. One I won't make again. I will be picking up a new set of intake seals next week and put it all back together. With luck (I am due for some good luck) I will be able to get the car running just right.

Richard.

68mustang351w
Gearhead

Posts: 558
From: San Jose, Ca
Registered: Sep 2004

posted 06-04-2006 09:38 PM     Click Here to See the Profile for 68mustang351w        Reply w/Quote
Umm... I didnt use any silicone on the other passages either. I only used a small amount around the water passages. What I would do when you re-install it is, install a few (four) studs on the heads and use them to align the intake. You could have accidentally moved them out of position when you installed the intake the last time. If youre not using studs, you can go to home depot and pick up some all thread and use that. Good luck, sounds like you are almost done (crosses fingers)... David F.

on edit: remember to use the correct tightening sequence and a torque wrench when you are ready to install it. When you are done, run the engine until its fully warm turn it off and retorque the intake. You might have to do that a couple of times. Keep us posted.

[This message has been edited by 68mustang351w (edited 06-04-2006).]

68 S-code GT
Gearhead

Posts: 3835
From: Sayreville, NJ, US
Registered: Mar 2000

posted 06-05-2006 08:31 AM     Click Here to See the Profile for 68 S-code GT        Reply w/Quote
It depends on which brand and type of gasket you get. Some of the Fel-Pro ones have what they call Printoseal on them. I think it’s a thin bead of silicon that is put on when the gasket is made.

FSTBK65
Gearhead

Posts: 483
From: Salem, Virginia 24153
Registered: May 2004

posted 06-05-2006 09:34 AM     Click Here to See the Profile for FSTBK65        Reply w/Quote
Permaseal not printoseal

buening
Gearhead

Posts: 317
From: Decatur, IL
Registered: Mar 2005

posted 06-05-2006 05:11 PM     Click Here to See the Profile for buening        Reply w/Quote
A quick tip that i use whenever installing new intake gaskets: Bring one of the intake manifold bolts with you to a hardware store and buy a few that are a couple inches longer. Cut the heads off the new bolts and thread them into the heads. These will act as guides for when you set the intake on the motor. I like to use the sealant on the head, then set the gaskets on the head (studs will now hold the gaskets in place), then put sealant on the gasket, then set the manifold and tighten per sequence and specs in the manuals. You will have to remove the studs one at a time whenever you get to that particular bolt in the torque sequence and replace with the correct intake bolt. I only put silicon around the water passages and use a thick bead on the ends of the intake. I do not use the cork end gaskets. Just make sure the bead is thick enough After you have all of the bolts torqued down, wait a 24 hours and then retorque. Start the motor up till it is warm, turn it back off and then retorque as necessary. Haven't had one leak this way yet! Just make sure that the mating surfaces of the head and intake are super clean. I like to use brake cleaner to get it nice and clean. If there is still gasket and silicone then get out a razor blade and carefully scrape it off (not getting any in the engine). One other tip is when putting silicone on the intake gaskets, put a dab on your fingertip and rub it on the gasket. This prevents getting too much silicone on the gasket and plugging things up. Just a thin even coat around the water passages is good. Hope this helps!

------------------
1970 Grabber Blue Mach 1 H-code
1970 Fastback
2003 Torch Red Mustang

johnmustang
Gearhead

Posts: 6748
From: British Columbia , Canada
Registered: Nov 2001

posted 06-06-2006 11:03 PM     Click Here to See the Profile for johnmustang        Reply w/Quote
Any luck yet? What is the verdict?

------------------
JOHN
65 FASTBACK 2+2
87 TAURUS WAGON
03 F150 XLT SUPER CREW 4X4 SHORT BOX
Member: PACIFIC COAST MUSTANG ASSOCIATION
Member:Vancouver Island Mustang Association
M&M #1710
65 FASTBACK
2003 F150 XLT SUPER CREW 4X4

rmousir
Gearhead

Posts: 1124
From: Amelia, Ohio
Registered: May 2003

posted 06-07-2006 08:15 AM     Click Here to See the Profile for rmousir        Reply w/Quote
quote:
Originally posted by johnmustang:
Any luck yet? What is the verdict?


I am picking up the new gaskets tonight from the local autozone. Felpro. Also need some break cleaner so I can finish the clean up. Should have it back together by this weekend.

When I took off the intake I could see that the seals did not 'seal' so I am feeling very confident that I found my problem. I will post all of the mistakes i made with this project when I get the car running. I was thinking about it yesterday and I can't believe that i have not sold the car yet. You guys really keep me going on this.

thanks.

Richard.

johnmustang
Gearhead

Posts: 6748
From: British Columbia , Canada
Registered: Nov 2001

posted 06-07-2006 09:17 AM     Click Here to See the Profile for johnmustang        Reply w/Quote
quote:
Originally posted by rmousir:
I was thinking about it yesterday and I can't believe that i have not sold the car yet. You guys really keep me going on this.

thanks.

Richard.


If we all sold our cars after making a few mistakes then none of us would own a classic mustang. We have all "done that been there" don`t feel bad it is just part of the learning curve.

I can guarantee that we all still make a bunch of mistakes (at least I do) but that is part of the fun (I think)

------------------
JOHN
65 FASTBACK 2+2
87 TAURUS WAGON
03 F150 XLT SUPER CREW 4X4 SHORT BOX
Member: PACIFIC COAST MUSTANG ASSOCIATION
Member:Vancouver Island Mustang Association
M&M #1710
65 FASTBACK
2003 F150 XLT SUPER CREW 4X4

SteveLaRiviere
Administrator

Posts: 48752
From: Saco, Maine
Registered: May 99

posted 06-07-2006 07:24 PM     Click Here to See the Profile for SteveLaRiviere        Reply w/Quote
quote:
Originally posted by rmousir:
When I took off the intake I could see that the seals did not 'seal' so I am feeling very confident that I found my problem.

A telltale sign of a leaking intake gasket is oil in the intake ports of the heads.

------------------
'70 Mustang Mach 1 - '70 Mustang Convertible - '72 Mustang Sprint - '94 F-150 XL

Jake11
Gearhead

Posts: 246
From: Banning,Ca,USA
Registered: Oct 2005

posted 06-07-2006 07:26 PM     Click Here to See the Profile for Jake11        Reply w/Quote

Don't give up. Your not beat yet. You got
people pulling for you. I'm one of them.
When things go wrong, just take a step back
and look at what went wrong. It is, after
all a learning experience. Make the most of
it and get her done. Then reap the rewards.

It will be worth all the trouble. I have
been there too. I think we all have.

KeithP

Aussie XAXB
Gearhead

Posts: 131
From: North Olmsted, Ohio
Registered: Jan 2006

posted 06-07-2006 09:35 PM     Click Here to See the Profile for Aussie XAXB        Reply w/Quote
Yes, there are Felpro gaskets termed "Printoseal". Edelbrock recommends them with their intakes. I used them on my wife's engine with no problem.

As someone mentioned be sure to follow proper torque sequence. Also I noticed after partially tightening the screws and them torquing them to specs that they all needed "clicking off" with the torque wrench a second or third time as the intake snugs down between the heads and the gaskets compress. Don't forget the washers too.

Steve

68 S-code GT
Gearhead

Posts: 3835
From: Sayreville, NJ, US
Registered: Mar 2000

posted 06-08-2006 07:51 AM     Click Here to See the Profile for 68 S-code GT        Reply w/Quote
quote:
Originally posted by FSTBK65:
Permaseal not printoseal

Well I think someone made a gasket some point in time and they called it that. Maybe it was Fel-Pro and maybe it wasn’t. It could have been phased out also for a better design and name.

buening
Gearhead

Posts: 317
From: Decatur, IL
Registered: Mar 2005

posted 06-08-2006 10:09 AM     Click Here to See the Profile for buening        Reply w/Quote
quote:
Originally posted by 68 S-code GT:
Well I think someone made a gasket some point in time and they called it that. Maybe it was Fel-Pro and maybe it wasn’t. It could have been phased out also for a better design and name.


Could you be thinking of Permagasket (the silicone sealant)? Another thing to point out is to be sure that your torque wrench is calibrated. I used one of the click torque wrenches and tested it with the bar type and found it to be WAAYYY off. I use an in-lb beam type torque wrench on my intake bolts, since the torque requirement is pretty small. Be sure to multiply by 12 to convert ft-lb into in-lb.

------------------
1970 Grabber Blue Mach 1 H-code
1970 Fastback
2003 Torch Red Mustang

68 S-code GT
Gearhead

Posts: 3835
From: Sayreville, NJ, US
Registered: Mar 2000

posted 06-09-2006 06:04 PM     Click Here to See the Profile for 68 S-code GT        Reply w/Quote
Fel-Pro gasket at Jegs! The 1250 & 1262 gaskets have what they call Printoseal!

https://www.jegs.com/webapp/wcs/stores/servlet/CategoryDi splay?lang=-1&catalogId=10002&storeId=10001&categoryId=16061

[img]https://www.jegs.com/images/photos/300/375/375-1250.jpg[/img]

https://www.jegs.com/images/photos/300/375/375-1250.jpg

[This message has been edited by 68 S-code GT (edited 06-09-2006).]

[This message has been edited by 68 S-code GT (edited 06-09-2006).]

rmousir
Gearhead

Posts: 1124
From: Amelia, Ohio
Registered: May 2003

posted 06-10-2006 07:27 PM     Click Here to See the Profile for rmousir        Reply w/Quote
GOOD NEWS!!!

I swapped out the intake seals and redid them. Put it all back together and got a chance to fire her up last night. Still had the same vacume leak that I had before but no surging or back firing. So I was a little frustrated.

So I called my wifes uncle. He is a old car guy. He comes buy and asks me a string of questions and then sees that I have 2 barrel carb on the 4 barrel intake with the adapter. He told me the adapters are big leakers. Told me that I most likely had a vacuum leak on the intake seals when I had the 4 barrel on there but had no idea why it was surging and back firing. After I put on the 2bl with the adapter the surging was gone but I still had the vacuum leak with was most likly the adapter/spacer that I was using.

He pulled out a Holley carb that he brought, poped it on. Started the car up. Ran with no problems. Adjusted the idel screw a little. Told me to get a new carb and that I could borrow his until I did.

Took the car out this morning and droveit about 10 miles or so, filled it up with gas. I have to tighten the one muffler clamp but other than that the car ran very well. Ideled nice, was powerful, responded nice. It has never driven this well for me since I have had it. You were right, I could feel the difference in the motor. Did a little burn out and was very happy with it.


Thanks for the help everyone. Especially ScottH. He was a huge part of me getting through this.


Richard.

SteveLaRiviere
Administrator

Posts: 48752
From: Saco, Maine
Registered: May 99

posted 06-10-2006 07:30 PM     Click Here to See the Profile for SteveLaRiviere        Reply w/Quote
Cool beans. Good job sticking it out and getting to the bottom of the problem. That's what being a gearhead is all about.

------------------
'70 Mustang Mach 1 - '70 Mustang Convertible - '72 Mustang Sprint - '94 F-150 XL

Fastymz
Moderator

Posts: 22791
From: Reno Nv M&M #1240
Registered: Apr 2001

posted 06-10-2006 07:41 PM     Click Here to See the Profile for Fastymz        Reply w/Quote
Great job,now go for a nice drive.

------------------
oddly obsessed with big scoops on little Mustangs

HOOD HACKERS DELIGHT!
My Pics

65ponycar
Gearhead

Posts: 873
From: Dayton, OH
Registered: Jul 2003

posted 06-11-2006 09:04 PM     Click Here to See the Profile for 65ponycar        Reply w/Quote
Hey Richard -

Glad to hear you got it going!! I bet that is a great feeling, I finally got my EFI conversion completed (few small things left).

I still got that Holley 570 Street Avenger carburetor if you are interested... I could meet you somewhere halfway on I75 if you decide you want it. It should work well for your application, basically new (3000 miles, about year old now)...

68 Coop
Gearhead

Posts: 5847
From: Mesquite, NV. 89027
Registered: Oct 2004

posted 06-11-2006 09:43 PM     Click Here to See the Profile for 68 Coop        Reply w/Quote
Great news Richard, I know it feels good to get this behind you, so now you can start something else.

Aussie XAXB
Gearhead

Posts: 131
From: North Olmsted, Ohio
Registered: Jan 2006

posted 06-12-2006 10:23 PM     Click Here to See the Profile for Aussie XAXB        Reply w/Quote
Good to hear you got it worked out. These things can really be a deterant but sticking it out usually gets you a great feeling in the end.

Steve

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